Chesapeake Announces Results from Two Eagle Ford Ventures in Giddings Field
Drilling Activity Details
Burleson
TX
United States
Drilling Activity Summary
Description
Two Eagle Ford completions in Burleson County (RRC Dist. 3), Texas, were announced by Chesapeake Operating Inc. The Giddings Field wells were drilled from a pad in Section 8, Stephen F Austin Survey, A-65. The #1H Schoeneman C was drilled to 18,059 ft, 9,362 ft true vertical, and produced 1.332 Mbbl of oil, 581 Mcf of gas and 1.571 Mbbl of water per day. Tested on a 23/64-in. choke, the flowing tubing pressure was 923 psi, and the flowing casing pressure was 67 psi. Production is from perforations at 8,648-18,010 ft. The #3H Schoeneman C was drilled to 17,300 ft with a true vertical depth of 8,654 ft. It produced 1.143 Mbbl of oil, 521 Mcf of gas and 1.58 Mbbl of water per day from perforations at 8,594-17,248 ft. Gauged on a 25/64-in. choke, the flowing tubing pressure was 751 psi, and the flowing casing pressure was 575 psi.
Two Eagle Ford completions in Burleson County (RRC Dist. 3), Texas, were announced by Chesapeake Operating Inc. The Giddings Field wells were drilled from a pad in Section 8, Stephen F Austin Survey, A-65. The #1H Schoeneman C was drilled to 18,059 ft, 9,362 ft true vertical, and produced 1.332 Mbbl of oil, 581 Mcf of gas and 1.571 Mbbl of water per day. Tested on a 23/64-in. choke, the flowing tubing pressure was 923 psi, and the flowing casing pressure was 67 psi. Production is from perforations at 8,648-18,010 ft. The #3H Schoeneman C was drilled to 17,300 ft with a true vertical depth of 8,654 ft. It produced 1.143 Mbbl of oil, 521 Mcf of gas and 1.58 Mbbl of water per day from perforations at 8,594-17,248 ft. Gauged on a 25/64-in. choke, the flowing tubing pressure was 751 psi, and the flowing casing pressure was 575 psi.