Chesapeake Operating Completes Two Eagle Ford Ventures in Texas’ McMullen County
Drilling Activity Details
Mc Mullen
TX
United States
Drilling Activity Summary
Description
Two Mc Mullen County (RRC Dist. 1), Texas, Eagle Ford wells were completed by Oklahoma City-based Chesapeake Operating Inc. The Eagleville Field discoveries were drilled from a pad in Section 23, J A Poitevent Survey, A-388 and both bottomed to the northwest in Section 3, Susan Skinner Survey, A-815. The #3HQ McKenzie HC 3 was drilled to 22,454 ft (9,959 ft true vertical). It flowed 1,089 bbl of oil, 655,000 cu ft of gas and 1,213 bbl of water daily from perforations at 10,590-22,397 ft. Gauged on a 21/64-in. choke, the flowing tubing pressure was 2,057 psi. The #4HQ McKenzie HC4 was drilled to 22,428 ft (9,953 ft true vertical). It produced 1,642 bbl of oil, 941,000 cu ft of gas and 681 bbl of water per day from perforations at 10,641-22,339 ft. Tested on an 18/64-in. choke, the flowing tubing pressure was 1,946 psi and the flowing casing pressure was 119 psi.
Two Mc Mullen County (RRC Dist. 1), Texas, Eagle Ford wells were completed by Oklahoma City-based Chesapeake Operating Inc. The Eagleville Field discoveries were drilled from a pad in Section 23, J A Poitevent Survey, A-388 and both bottomed to the northwest in Section 3, Susan Skinner Survey, A-815. The #3HQ McKenzie HC 3 was drilled to 22,454 ft (9,959 ft true vertical). It flowed 1,089 bbl of oil, 655,000 cu ft of gas and 1,213 bbl of water daily from perforations at 10,590-22,397 ft. Gauged on a 21/64-in. choke, the flowing tubing pressure was 2,057 psi. The #4HQ McKenzie HC4 was drilled to 22,428 ft (9,953 ft true vertical). It produced 1,642 bbl of oil, 941,000 cu ft of gas and 681 bbl of water per day from perforations at 10,641-22,339 ft. Tested on an 18/64-in. choke, the flowing tubing pressure was 1,946 psi and the flowing casing pressure was 119 psi.