Des Moines Granite Wash Well: 112 boc, 4.58 MMcf/d.
Drilling Activity Details
TX
United States
Drilling Activity Summary
Description
Tulsa-based Unit Petroleum Co. completed a Hemphill (RRC Dist. 10), Texas, Des Moines Granite Wash venture. The #4H Dixon 5554 CXL is producing 4.58 MMcf of gas, 112 bbl of 48-degree-gravity condensate and 3.787 Mbbl of water per day. It is in Section 56, Block M-1, H&GN Survey, and production is from a fracture-stimulated lateral at 12,352-19,817 ft. Unit drilled the well to 19,830 ft, 12,059 ft true vertical, and it bottomed to the southeast in Section 54, A-1167. Gauged on a 128/64-in. choke, the flowing tubing pressure was 1,412 psi and the shut-in tubing pressure was 1,442 psi.
Tulsa-based Unit Petroleum Co. completed a Hemphill (RRC Dist. 10), Texas, Des Moines Granite Wash venture. The #4H Dixon 5554 CXL is producing 4.58 MMcf of gas, 112 bbl of 48-degree-gravity condensate and 3.787 Mbbl of water per day. It is in Section 56, Block M-1, H&GN Survey, and production is from a fracture-stimulated lateral at 12,352-19,817 ft. Unit drilled the well to 19,830 ft, 12,059 ft true vertical, and it bottomed to the southeast in Section 54, A-1167. Gauged on a 128/64-in. choke, the flowing tubing pressure was 1,412 psi and the shut-in tubing pressure was 1,442 psi.