Eagle Ford Discovery Tested Flowing 35.4 MMcf Of Gas Per Day
Drilling Activity Details
Dimmit
TX
United States
Drilling Activity Summary
Description
Chesapeake Operating Inc. completed an Eagle Ford producer in Briscoe Ranch Field in Dimmit County (RRC Dist. 1), Texas. The #4BH Big Wells South Unit 10 was tested flowing 35.4 MMcf of gas per day from perforations at 7,541-16,070 ft after acidizing and fracturing. It was drilled to 16,186 ft, and the true vertical depth is 7,128 ft. It is in Korn Valentine Survey, A-1179, and bottomed in Gallagher Dominic Survey, A-74. The discovery was tested on a 17/64-in. choke, and the flowing tubing pressure was 781 psi. Chesapeake is based in Oklahoma City.
Chesapeake Operating Inc. completed an Eagle Ford producer in Briscoe Ranch Field in Dimmit County (RRC Dist. 1), Texas. The #4BH Big Wells South Unit 10 was tested flowing 35.4 MMcf of gas per day from perforations at 7,541-16,070 ft after acidizing and fracturing. It was drilled to 16,186 ft, and the true vertical depth is 7,128 ft. It is in Korn Valentine Survey, A-1179, and bottomed in Gallagher Dominic Survey, A-74. The discovery was tested on a 17/64-in. choke, and the flowing tubing pressure was 781 psi. Chesapeake is based in Oklahoma City.