Hughes County, Okla., Completions Flow from Commingled Woodford, Mayes
Drilling Activity Details
Hughes
OK
United States
Drilling Activity Summary
Description
In Hughes County, Okla., Calyx Energy III completed two Carson Field wells in Section 14-8n-12e. The #4-14-26WH Hamilton produced 9.21 MMcf of gas and 4,004 bbl of water daily from commingled Mayes (5,193-14,214 ft) and Woodford (5,349-15,761ft). The well was drilled to 15,850 ft with a true vertical depth of 4,893 ft. It was tested on a 64/64-inch choke, and the flowing tubing pressure was 368 psi. The #2-14-26WH Hamilton was drilled to 15,852 ft, 4,954 ft true vertical. It initially flowed 7.781 MMcf of gas and 3,788 bbl of water per day from commingled Woodford and Mayes at 5,201-15,766 ft. Gauged on a 64/64-inch choke, the flowing tubing pressure was 279 psi. Calyx Energy is based in Tulsa.
In Hughes County, Okla., Calyx Energy III completed two Carson Field wells in Section 14-8n-12e. The #4-14-26WH Hamilton produced 9.21 MMcf of gas and 4,004 bbl of water daily from commingled Mayes (5,193-14,214 ft) and Woodford (5,349-15,761ft). The well was drilled to 15,850 ft with a true vertical depth of 4,893 ft. It was tested on a 64/64-inch choke, and the flowing tubing pressure was 368 psi. The #2-14-26WH Hamilton was drilled to 15,852 ft, 4,954 ft true vertical. It initially flowed 7.781 MMcf of gas and 3,788 bbl of water per day from commingled Woodford and Mayes at 5,201-15,766 ft. Gauged on a 64/64-inch choke, the flowing tubing pressure was 279 psi. Calyx Energy is based in Tulsa.