Mississippian Discovery Tested Flowing 978 bbl of Oil, 1.545 MMcf of Gas, per Day
Drilling Activity Details
Locations
Grady
OK
United States
Operators
Plays
Post Date
Shore Type
Well Name
#1H-31 AR-JO McComas
Geo Coordinate
Drilling Activity Summary
Description
Citizen Energy III announced results from a Grady County, Okla., completion. The #1H-31 AR-JO McComas initially flowed 158 bbl of 53° API condensate, 1.545 MMcf of gas and 978 bbl of water per day from Mississippian. The Watonga-Chickasha Trend well was drilled in Section 31-10n-7w to a total depth of 17,210 ft and a true vertical depth of 12,061 ft. Gauged on 22/64-inch choke, the flowing tubing pressure was 1,569 psi. Production is from a perforated zone at 12,180-17,139 ft. Citizen Energy’s headquarters are in Tulsa.
Description
Citizen Energy III announced results from a Grady County, Okla., completion. The #1H-31 AR-JO McComas initially flowed 158 bbl of 53° API condensate, 1.545 MMcf of gas and 978 bbl of water per day from Mississippian. The Watonga-Chickasha Trend well was drilled in Section 31-10n-7w to a total depth of 17,210 ft and a true vertical depth of 12,061 ft. Gauged on 22/64-inch choke, the flowing tubing pressure was 1,569 psi. Production is from a perforated zone at 12,180-17,139 ft. Citizen Energy’s headquarters are in Tulsa.