Results from Two Squaw Field-McKenzie County, N.D., Ventures Announced by WPX Energy
Drilling Activity Details
McKenzie
ND
United States
Drilling Activity Summary
Description
WPX Energy Inc. completed two McKenzie County, N.D., Williston Basin wells. The Squaw Field wells were drilled from a pad in Section 25-149n-95w. The #24-13-12HIL Omaha Woman was drilled to 26,767 ft (11,004 ft true vertical). It flowed 3,720 bbl of 42°API oil with 1.237 MMcf of gas and 1,612 bbl of water per day from fractured Middle Bakken perforations at 11,603-26,672 ft. Tested on a 28/64-inch choke, the flowing casing pressure was 2,950 psi. The #24-13-12HY Omaha Woman was drilled to 26,763 ft, and the true vertical depth is 11,207. The Three Forks producer flowed 4,794 bbl of 42° API oil, 2.637 MMcf of gas and 8,364 bbl of water per day. Tested on a 52/64-inch choke, the flowing casing pressure was 2,850 psi, and production is from a fracture stimulated zone at 11,627-26,602 ft. WPX is based in Tulsa.
WPX Energy Inc. completed two McKenzie County, N.D., Williston Basin wells. The Squaw Field wells were drilled from a pad in Section 25-149n-95w. The #24-13-12HIL Omaha Woman was drilled to 26,767 ft (11,004 ft true vertical). It flowed 3,720 bbl of 42°API oil with 1.237 MMcf of gas and 1,612 bbl of water per day from fractured Middle Bakken perforations at 11,603-26,672 ft. Tested on a 28/64-inch choke, the flowing casing pressure was 2,950 psi. The #24-13-12HY Omaha Woman was drilled to 26,763 ft, and the true vertical depth is 11,207. The Three Forks producer flowed 4,794 bbl of 42° API oil, 2.637 MMcf of gas and 8,364 bbl of water per day. Tested on a 52/64-inch choke, the flowing casing pressure was 2,850 psi, and production is from a fracture stimulated zone at 11,627-26,602 ft. WPX is based in Tulsa.