Trinity Operating Completes Mayes, Woodford Producers at Pad in Hughes County, Okla.
Drilling Activity Details
Hughes
OK
United States
Drilling Activity Summary
Description
Three Hughes County, Okla., completions were reported by Houston-based Trinity Operating Inc. The wells were drilled from a pad in Section 5-7n-12e. The #2-32/29H Mitzi initially flowed 6.33 MMcf of gas and 2.112 Mbbl of water per day from an acidized and fractured zone in Mayes at 14,226-14,422 ft. The 15,680-ft venture presumably has been perforated and treated in the Woodford as well, but little information has been released. The #4-32/29H Mitzi was drilled about 15 ft north on the pad and has been perforated, acidized and fractured in Woodford at 6,009-10,026 ft and 10,713-13,617 ft, and Mayes at 14,139-14,140 ft; however, an initial production rate was not reported. The #3-32/29H Mitzi was tested flowing 3.29 MMcf of gas and 1.584 Mbbl of water per day from Woodford between 5,096 and 15,300 ft. The flowing tubing pressure was 280 psi when tested on an open choke. The three wells were drilled with parallel laterals extending north across Section 32-8n-12e with bottomhole locations in Section 29-8n-12e. According to the company, core analysis indicates the Woodford underlying sections 29 and 32 have average net effective pay of about 80 ft, and it calculated that the two-section unit contained recoverable original gas-in-place of approximately 24.6 Bcf.
Three Hughes County, Okla., completions were reported by Houston-based Trinity Operating Inc. The wells were drilled from a pad in Section 5-7n-12e. The #2-32/29H Mitzi initially flowed 6.33 MMcf of gas and 2.112 Mbbl of water per day from an acidized and fractured zone in Mayes at 14,226-14,422 ft. The 15,680-ft venture presumably has been perforated and treated in the Woodford as well, but little information has been released. The #4-32/29H Mitzi was drilled about 15 ft north on the pad and has been perforated, acidized and fractured in Woodford at 6,009-10,026 ft and 10,713-13,617 ft, and Mayes at 14,139-14,140 ft; however, an initial production rate was not reported. The #3-32/29H Mitzi was tested flowing 3.29 MMcf of gas and 1.584 Mbbl of water per day from Woodford between 5,096 and 15,300 ft. The flowing tubing pressure was 280 psi when tested on an open choke. The three wells were drilled with parallel laterals extending north across Section 32-8n-12e with bottomhole locations in Section 29-8n-12e. According to the company, core analysis indicates the Woodford underlying sections 29 and 32 have average net effective pay of about 80 ft, and it calculated that the two-section unit contained recoverable original gas-in-place of approximately 24.6 Bcf.