Two Austin Chalk-Giddings Field Wells Completed by Ramtex Energy
Drilling Activity Details
Fayette
TX
United States
Drilling Activity Summary
Description
Ramtex Energy, based in Tulsa, Okla., announced results from two Austin Chalk completions in Giddings Field. The discoveries were drilled from a pad in Fayette County (RRC Dist. 3), Texas, in William O. Burnham Survey, A-124. The #1H Hawk produced 10.434 MMcf of gas and 426 bbl of oil with 1.59 Mbbl of water per day. The 21,131-ft well has a true vertical depth of 13,885 ft. It was tested on a 7/64-in. choke with a flowing tubing pressure of 3,482 psi and a shut-in tubing pressure of 5,700 psi. Production is from perforations at 14,703-20,913 ft. The #1H Lincoln was drilled to 19,900 ft, 13,393 ft true vertical, and produced 635 bbl of oil, 13.767 MMcf of gas and 1.848 Mbbl of water per day. Production is from perforations at 14,329-19,788 ft. Gauged on a 28/64-in. choke, the flowing casing pressure was 3,979 psi, and the shut-in casing pressure was 4,407 psi.
Ramtex Energy, based in Tulsa, Okla., announced results from two Austin Chalk completions in Giddings Field. The discoveries were drilled from a pad in Fayette County (RRC Dist. 3), Texas, in William O. Burnham Survey, A-124. The #1H Hawk produced 10.434 MMcf of gas and 426 bbl of oil with 1.59 Mbbl of water per day. The 21,131-ft well has a true vertical depth of 13,885 ft. It was tested on a 7/64-in. choke with a flowing tubing pressure of 3,482 psi and a shut-in tubing pressure of 5,700 psi. Production is from perforations at 14,703-20,913 ft. The #1H Lincoln was drilled to 19,900 ft, 13,393 ft true vertical, and produced 635 bbl of oil, 13.767 MMcf of gas and 1.848 Mbbl of water per day. Production is from perforations at 14,329-19,788 ft. Gauged on a 28/64-in. choke, the flowing casing pressure was 3,979 psi, and the shut-in casing pressure was 4,407 psi.