Two Mancos Discoveries Announced In San Juan Basin
Drilling Activity Details
Drilling Activity Summary
Description
London-based BP Plc announced results from two horizontal Mancos producers in the San Juan Basin portion of San Juan County, N.M. The #604-2H NEBU Com, Section 13-31n-7w, produced an average of 8.83 MMcf of gas per day. It was drilled eastward to 17,193 ft and bottomed in Section 18-31n-6w with a true vertical depth of 7,089 ft. It was tested on an 18/64-in. choke following 48-stage fracturing between 7,397 and 16,991 ft and the flowing casing pressure was 1,900 psi. About one-half mile south is #602-1H NEBU Com in Section 12-31n-7w. The discovery had an average 30-day initial production rate of 12.9 MMcf of gas per day. It was tested on an 18/64-in. choke following 64-stage acidizing and fracturing between 7,760 and 17,306 ft and the flowing casing pressure was 1,550 psi. It was horizontally drilled east to 17,517 ft and bottomed in Section 7-31n-7w. The true vertical depth is 7,065 ft.
London-based BP Plc announced results from two horizontal Mancos producers in the San Juan Basin portion of San Juan County, N.M. The #604-2H NEBU Com, Section 13-31n-7w, produced an average of 8.83 MMcf of gas per day. It was drilled eastward to 17,193 ft and bottomed in Section 18-31n-6w with a true vertical depth of 7,089 ft. It was tested on an 18/64-in. choke following 48-stage fracturing between 7,397 and 16,991 ft and the flowing casing pressure was 1,900 psi. About one-half mile south is #602-1H NEBU Com in Section 12-31n-7w. The discovery had an average 30-day initial production rate of 12.9 MMcf of gas per day. It was tested on an 18/64-in. choke following 64-stage acidizing and fracturing between 7,760 and 17,306 ft and the flowing casing pressure was 1,550 psi. It was horizontally drilled east to 17,517 ft and bottomed in Section 7-31n-7w. The true vertical depth is 7,065 ft.